wcuhillbilly
Member
- 421
- 5
- 18
- Location
- Devils Tower, WY
Trying to upload the pics to Photobucket but its being a butt. 2hrs and only one pic is up,,, sizes are correct. Electronics will insult your intelligence, but nothing rubs it in like a computor.
here is the beast as it sits. Truck weighing in at 36k and the dozer/trailer, putting the combo up near 60K+ I felt it was time to invest in some whoa and go. As some of you know I scored an old NTC 350 sometime back for scrap. This gave me manifolds, turbo (VT50) 25A Jakes and alot of fittings etc.
After scrapping the turbo, I talked to Blaylock Turbo in KS and settled on a Schwitzer 4LHR for a good deal. Rebuilt the jakes with a kit from Cummins and one new solenoid. I finally got around to attempting to put this mess together this past week.
Scored the aftercooler/ watercooled intake as well.
So being I had 4 days off last week I decided to start into just put the jakes on last tuesday, I could not have known how wrong I would be thinking this would be about a day, and some wiring........
So I got the rocker boxes off and swapped the crossheads,(for those who dont know, this is the bar that rides on a post allowing the rocker to push both valves at the same time. The Jake version is wider so the jake can push the valves while allowing the rocker to follow the pushrod)
Checked the plugs in the intake/head, (plugged already whoo hoo!)
started re-assembly of rocker boxes (mind you I was only going to do the rear heads as the original plan was to only be down a day.....)
Once I had the middle jake in place I started working on the rear head. Figured this would be the closest I would get to the plug for the duel fuel mod, thus it would be wise to get the plug moving now versus later. after torturing a 3/16 allen key almost to a 90* twist and a bend, the plug was moving enough for my satisfaction.. the return plug would not budge... no worries,,,
here is the beast as it sits. Truck weighing in at 36k and the dozer/trailer, putting the combo up near 60K+ I felt it was time to invest in some whoa and go. As some of you know I scored an old NTC 350 sometime back for scrap. This gave me manifolds, turbo (VT50) 25A Jakes and alot of fittings etc.
After scrapping the turbo, I talked to Blaylock Turbo in KS and settled on a Schwitzer 4LHR for a good deal. Rebuilt the jakes with a kit from Cummins and one new solenoid. I finally got around to attempting to put this mess together this past week.
Scored the aftercooler/ watercooled intake as well.
So being I had 4 days off last week I decided to start into just put the jakes on last tuesday, I could not have known how wrong I would be thinking this would be about a day, and some wiring........
So I got the rocker boxes off and swapped the crossheads,(for those who dont know, this is the bar that rides on a post allowing the rocker to push both valves at the same time. The Jake version is wider so the jake can push the valves while allowing the rocker to follow the pushrod)
Checked the plugs in the intake/head, (plugged already whoo hoo!)
started re-assembly of rocker boxes (mind you I was only going to do the rear heads as the original plan was to only be down a day.....)
Once I had the middle jake in place I started working on the rear head. Figured this would be the closest I would get to the plug for the duel fuel mod, thus it would be wise to get the plug moving now versus later. after torturing a 3/16 allen key almost to a 90* twist and a bend, the plug was moving enough for my satisfaction.. the return plug would not budge... no worries,,,
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