AndrewH
Member
- 376
- 1
- 18
- Location
- Boyne City MI
My '09 has been trying to die for awhile it seems. I noticed it smoking and missing around thanksgiving. I pulled the RH head and found the valves werent perfect. I had done a compression test but I'll not include that here because I found my tester was doo-doo. New head and new gaskets ect and back together. Still some smoke and some missing. I left it alone because that is my plow truck and I was lazy. Well in case no one has notices we never really got winter. So I pulled the truck in and tore it down again. I had a ton of blowby by now coming from the rocker covers and the oil fill. This time I had a good compression tester. 410 accrpss the entire LH bank. 410 on 2 and 6 RH bank. Less than 100 on 6 and 8. I found 6 and 8 both had cracked the pistons. 6 parallell with the wristpin right through the middle of the head of the piston and 8 was almost 90 degrees different. The crack running up and down. In both cases the piston had pinched the rings and not allowed them to move. I'll get you some pictures. So my question is this : If it was water in the fuel why didnt I kill all of them? Or was it something else?