During a 500 mile Road Trip I experienced what felt like stuck-in 2nd on the freeway. The sound just did not seem high enough, and there was a floor felt rumble. I thought I might not yet have shifted into 3rd. After sever miles, the pitch went up and, at least felt like 3rd.
Any reason to believe that the rear main leak could affect 2nd-to-3rd shift issues?
Hose inspection will be done Friday in case the heat from the engine is collapsing oil-soaked trans modulator line?
Anything else?
Any reason to believe that the rear main leak could affect 2nd-to-3rd shift issues?
Hose inspection will be done Friday in case the heat from the engine is collapsing oil-soaked trans modulator line?
Anything else?