My '08 caught on fire this morning. This truck has never missed a beat despite what it's been thru. During the last week my glowplug system had been acting funny. By funny I mean it was holding relay closed for a long long time compared to what it had been. The resistor pack started to smoke one morning it stayed on so long. I was able to get out and check the relay. It wasn't stuck. The card was holding it on.
The GP's were 2 years old so I decided to change all 8 and check the rest of the system. I followed the TM's. Everything checked out fine except the resistor. TM said .28 ohms (which seems really low) and mine measured at 1.4ohms. I decided it was time to bypass it since everyone does anyway.
While I was at it I did the doghead stater relay mod just because a few days prior the OE starter relay failed to engage(or so I thought). I figured it was on borrowed time so I changed that too. I drove the truck a few times after the dohead mod and everything seemed GTG.
This morning I cycled the key let the GP card so it's thing. Everything seemed ok. I turned the key to start...and nothing. Then I heard a bang and a lot of smoke rolled up from under the hood from the GP relay area. I got out to check and the wiring behind the driver-side cyl head was on fire. The house and the garage were locked up so I put it out with the dogs water dish. I know, I know...water on an electrical fire. I didn't get a chance to sort thru the mess as all the running around like a maniac made me late for work.
All I can say is FHGSGFHGSGFH! I've been on the forum as long as I've had the truck. I've read some interesting things and I've always thought "man I'm lucky everything on mine works!"
The GP's were 2 years old so I decided to change all 8 and check the rest of the system. I followed the TM's. Everything checked out fine except the resistor. TM said .28 ohms (which seems really low) and mine measured at 1.4ohms. I decided it was time to bypass it since everyone does anyway.
While I was at it I did the doghead stater relay mod just because a few days prior the OE starter relay failed to engage(or so I thought). I figured it was on borrowed time so I changed that too. I drove the truck a few times after the dohead mod and everything seemed GTG.
This morning I cycled the key let the GP card so it's thing. Everything seemed ok. I turned the key to start...and nothing. Then I heard a bang and a lot of smoke rolled up from under the hood from the GP relay area. I got out to check and the wiring behind the driver-side cyl head was on fire. The house and the garage were locked up so I put it out with the dogs water dish. I know, I know...water on an electrical fire. I didn't get a chance to sort thru the mess as all the running around like a maniac made me late for work.
All I can say is FHGSGFHGSGFH! I've been on the forum as long as I've had the truck. I've read some interesting things and I've always thought "man I'm lucky everything on mine works!"