Jimc
Member
- 725
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- 18
- Location
- Mullica, nj
a little update with my 003. at about 80% this thing has always started puffing black smoke that just got worse at 85-90-95. also, this whole time i thought the ammeter wasnt reading correct. the gen seemed to be putting out a ton of power and ran good. well, since i rebuilt an 002 and it ran so fantastic that for the **** of it i decided to pull the injectors from my 003 and send them out to storeman/jerry. so far he has done 12 injectors for me. 2-003's and 2-002's. i never bothered to do the injectors on my 003 because the previous owner said he sent them out and had them done just before i bought it. spec in the injectors is 1750psi. jerry found 3 injectors popping around 1400 and one was sticking and popping at 2200. he ordered one replacement nozzle for me for the sticking one and then tuned all to spec. package arrived today. i reinstalled the injectors with all new gaskets and got her up and running.
results: the first 15min of just running, no load, i didnt notice much of a difference. believe it or not it ran smooth before. there was some slight smoke but it wasn't hot yet. i hooked it up to my shop and started applying load. shudders opened, smoke cleared, ran great. prior to the injnectors being done i could run my 7.5hp compressor and once started i could add 8-4 tube flourescent fixtures. any more than that and i could stall out the gen and the black smoke would be chugging like crazy. now the compressor fires right up with only a split second reaction from the gen. before, rpms would die way down and take about 5 sec to recover. once the compressor was running i added 34 - 4 tube fluorescent fixtures and a 1500 watt infrared heater. now the ammeter is at 115% and pretty much no smoke from the exhaust. gen would stall out before at 90-95%. at one point something else kicked on in the shop, i think the refrigerator and the ammeter pegged at 133% and still no noticable difference or overloaded sound from the engine. no hint of stalling or black smoke.
this is all unbelievable. the output of this gen now is nuts. i cant believe this thing put out that much power and the reaction when a motor starts up it totally instant. at 133% its still going strong and i actually ran out of things to turn on. out of 4 generators there hasnt been a single injector that was set right or operating correctly. thats not really surprising. you would figure springs would get a little weak after 30 years and some adjustment would be needed. i can bet that most of you guys with 002s and 003s that have them running and never did the injectors, i bet you would be really surprised at how your gen ran after you had them tuned.
results: the first 15min of just running, no load, i didnt notice much of a difference. believe it or not it ran smooth before. there was some slight smoke but it wasn't hot yet. i hooked it up to my shop and started applying load. shudders opened, smoke cleared, ran great. prior to the injnectors being done i could run my 7.5hp compressor and once started i could add 8-4 tube flourescent fixtures. any more than that and i could stall out the gen and the black smoke would be chugging like crazy. now the compressor fires right up with only a split second reaction from the gen. before, rpms would die way down and take about 5 sec to recover. once the compressor was running i added 34 - 4 tube fluorescent fixtures and a 1500 watt infrared heater. now the ammeter is at 115% and pretty much no smoke from the exhaust. gen would stall out before at 90-95%. at one point something else kicked on in the shop, i think the refrigerator and the ammeter pegged at 133% and still no noticable difference or overloaded sound from the engine. no hint of stalling or black smoke.
this is all unbelievable. the output of this gen now is nuts. i cant believe this thing put out that much power and the reaction when a motor starts up it totally instant. at 133% its still going strong and i actually ran out of things to turn on. out of 4 generators there hasnt been a single injector that was set right or operating correctly. thats not really surprising. you would figure springs would get a little weak after 30 years and some adjustment would be needed. i can bet that most of you guys with 002s and 003s that have them running and never did the injectors, i bet you would be really surprised at how your gen ran after you had them tuned.
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