lurkMcGurk
Member
- 55
- 17
- 8
- Location
- Bangor,Maine
I cant speak for the customer service FLUfarm but everything is still running well on this end. Well I say everything but I mean as far as the Blue Devil is concerned. I got out to the area I flattened out a few days ago and had some 2-3 inch stone dropped off. I could not get it leveled enough before getting the stone delivered. I tried backdragging before the stone got dropped off with the mog. Backdragging was a bear and to be fair I had a ton of rock and stumpage and very little dirt to work with. Anyhow here is kind of a before without a clear view of the area behind Mog1.
and here is kind of an after shot after 35 cu yard finished
So the good news is I had it all flattened and the rocks moved across the area in short order. Kind of a juggling act to hit the pile and curl the bucket before the momentum wanted to choke out the engine but I figured it out in short order. All the while remembering the cartoon about not using the front as a bulldozer!
This area will be for some log milling and such and wont turn to mud as it should drain nicely.
All was going well and I was using the 4x4 switch (and making gentle K turns in rev and fwd) and then when I was about done I switched back to 2wd and to do some back dragging and then had some difficulty getting the switch to go back to 4x4. I replaced this switch as it was delivered broken and can only figure I'm probably kicking things loose inside the air lines and gumming up the works. I (like so many before me) will be diving into this in the near future. I drove over to my parking spot and shut everything down and noted this
from the passenger side rear. I saw this the other day and have checked the brake fluid 4x since and still full. I looked in the sight hole and even added more gear oil but it was already full or only needed a few oz because the excess weeped out the sight hole. It could be brakes or gear I'm not sure. I'm wondering if because (like an idiot) I left the P brake on while repositioning the backhoe the other day I caused some leakage, dunno. Mysteries abound. Most importantly on a flat level surface I was able to engage 4x4 again but after some jostling around and NO diff Lock. I suspect the air system and possible a slow leak in the brakes.
Mog 2 (Lord Voldemort) needed a 4x4 switch as well and one of the three holes the banjo fittings connect to looked crusty in there. I'm anticipating air line work will be needed here also . It has built pressure once and I do need to change the air release valves on the tanks and possibly a "solenoid? not sure if thats the parts name" for the front hydraulics that may have been leaky in the past. LV came with "significant blow by" from Gov Planet but I presume that was from the Texarkana custom exhaust crimping service down there. Opened it up and the smoke has cleared. found the paperwork and L.Voledemort had a new engine put in just before "Mission Putaway" in 2009. IDK what that means other than new engine,,,and I like that.
So i'm going to check out this infamous "low spot" in the air lines and see if it was ever replaced or if its clogged. Then I'll do some upstream downstream checks to maybe isolate the problem.
also need to take the wheel off some time and see where the leak is coming from on Mog1. This will happen with Mog 1 as soon as Ive addressed the issues with Mog 2 / LV. Those issues are a new 4x4 switch "meritor wabco ebay $175" possible a solenoid on the front hydraulics that looks leaky and all the pressure relief valves on the tanks that leak like a sieve. Still not regretting the route I took and have to believe with a Kubota at less than half the HP and more than twice the price id still be moving those rocks.
All in all I will be prioritizing keeping atleast one running at all times. I really like using this Mog to get real work done and I'm kind of thinking it wants to work as well. Keep you all posted and feel free to send me any info tips or thoughts as you like. Im cruising the threads here as a member and benzworld as a ghost but realize I miss some stuff as it gets posted.
and here is kind of an after shot after 35 cu yard finished
So the good news is I had it all flattened and the rocks moved across the area in short order. Kind of a juggling act to hit the pile and curl the bucket before the momentum wanted to choke out the engine but I figured it out in short order. All the while remembering the cartoon about not using the front as a bulldozer!
This area will be for some log milling and such and wont turn to mud as it should drain nicely.
All was going well and I was using the 4x4 switch (and making gentle K turns in rev and fwd) and then when I was about done I switched back to 2wd and to do some back dragging and then had some difficulty getting the switch to go back to 4x4. I replaced this switch as it was delivered broken and can only figure I'm probably kicking things loose inside the air lines and gumming up the works. I (like so many before me) will be diving into this in the near future. I drove over to my parking spot and shut everything down and noted this
from the passenger side rear. I saw this the other day and have checked the brake fluid 4x since and still full. I looked in the sight hole and even added more gear oil but it was already full or only needed a few oz because the excess weeped out the sight hole. It could be brakes or gear I'm not sure. I'm wondering if because (like an idiot) I left the P brake on while repositioning the backhoe the other day I caused some leakage, dunno. Mysteries abound. Most importantly on a flat level surface I was able to engage 4x4 again but after some jostling around and NO diff Lock. I suspect the air system and possible a slow leak in the brakes.
Mog 2 (Lord Voldemort) needed a 4x4 switch as well and one of the three holes the banjo fittings connect to looked crusty in there. I'm anticipating air line work will be needed here also . It has built pressure once and I do need to change the air release valves on the tanks and possibly a "solenoid? not sure if thats the parts name" for the front hydraulics that may have been leaky in the past. LV came with "significant blow by" from Gov Planet but I presume that was from the Texarkana custom exhaust crimping service down there. Opened it up and the smoke has cleared. found the paperwork and L.Voledemort had a new engine put in just before "Mission Putaway" in 2009. IDK what that means other than new engine,,,and I like that.
So i'm going to check out this infamous "low spot" in the air lines and see if it was ever replaced or if its clogged. Then I'll do some upstream downstream checks to maybe isolate the problem.
also need to take the wheel off some time and see where the leak is coming from on Mog1. This will happen with Mog 1 as soon as Ive addressed the issues with Mog 2 / LV. Those issues are a new 4x4 switch "meritor wabco ebay $175" possible a solenoid on the front hydraulics that looks leaky and all the pressure relief valves on the tanks that leak like a sieve. Still not regretting the route I took and have to believe with a Kubota at less than half the HP and more than twice the price id still be moving those rocks.
All in all I will be prioritizing keeping atleast one running at all times. I really like using this Mog to get real work done and I'm kind of thinking it wants to work as well. Keep you all posted and feel free to send me any info tips or thoughts as you like. Im cruising the threads here as a member and benzworld as a ghost but realize I miss some stuff as it gets posted.
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